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The test whistle sounded good on the very first attempt. I just drilled a hole at the end of the windway squared it up, filed the ramp, put in a plug and it worked immediately.
Anyway, I used a router with a 3/8" straight bit inside a 1/2" template bushing. I know that means it isn't truly concentric, but a little sanding could fix that. Having a straight clean roof at the right height to start with gets me past a major stumbling block. In its current form, it only works on tubes with a consistent diameter and wall thickness. Actually, changing the wall thickness would change the windway height. I am also using the router in a jig on my lathe to get consistent diameter.
Fairly self explanatory:
After taking the picture of the end of the whistle I realized I needed to clean it up after cutting the beak. The interior is smooth as glass.